Author Topic: Wasted main  (Read 3507 times)

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Offline larrym

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Wasted main
« on: October 09 2014, 05:35:58 PM »
So a buddy of mine had used motor he was installing in a roller he had. It was running when he pulled from the other car.
 He was just going to change the rear main on the stand and the bearings looked a little suspect we both felt it looked like contamination.
He pulled the crank and took it in for a polish apparently 1 rod journal was out of round. When we pulled it apart we saw no evidence on any rod bearings but the machinist is very anal so he had the rods turned .010 and the mains polished.
Put it together it lasted 3 weeks clearances were all around .020 when assembled and now one of the caps is loose in the register main bearing on the cap side is toast. It fit tight when assembled and needed a persuasion to come apart.
Rods seem fine so starvation seems unlikely   
Bent crank?
Cracked block?
Cracked crank?
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
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Offline Scoobum

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Re: Wasted main
« Reply #1 on: October 09 2014, 05:47:24 PM »
3.8? Steel or stock caps?
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Offline larrym

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Wasted main
« Reply #2 on: October 09 2014, 06:28:38 PM »
3.8 stock caps and fasteners
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

Offline Steve Wood

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Re: Wasted main
« Reply #3 on: October 09 2014, 08:08:45 PM »
sounds like the bolts lost tension and the cap walked
Steve Wood

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Offline larrym

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Wasted main
« Reply #4 on: October 09 2014, 08:30:04 PM »
They appeared to be torqued when disassembled I'm going to stop by and have a peek tonight. 
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

Offline TexasT

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Re: Wasted main
« Reply #5 on: October 09 2014, 11:06:10 PM »
Did he use a torque wrench to break em loose? That would tell a story if it didn't take much to break it loose.

Might torque the caps back on ans hit em with a  spring gauge across several different angles to see if any out of round.
Rich

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Offline larrym

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Wasted main
« Reply #6 on: October 09 2014, 11:12:49 PM »
I just left his place the 2 centre bears are cooked got very hot.
He said the fasteners were tight coming off. If there was an oiling issue would it not show on the rods also?
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

Offline Scoobum

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Re: Wasted main
« Reply #7 on: October 09 2014, 11:24:16 PM »
I'm very specific when I have my engines built. A machinist should check the mains with an elongated dial indicator. Each main is checked at 12, 3. 6 and 9 o'clock. If plastigauge showed evenly across the face of each main for clearance...an d the crank turned freely...then I'm at a loss to explain what happened. The main "tightened" up for some reason. The block, cap and crank will have to be magged for heat cracks.
Hard work pays off, dreams come true. Bad times don't last, but BAD GUYS do!

RIP Scott Hall AKA Razor Ramon

Offline Steve Wood

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Re: Wasted main
« Reply #8 on: October 09 2014, 11:25:43 PM »
No oil,  or too tight of clearance
Steve Wood

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A lot of broken parts does not make you a racer; it makes you a slow learner.

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Re: Wasted main
« Reply #9 on: October 09 2014, 11:28:25 PM »
Larry...ask your friend if those 2 caps have the chamfer in them that fit into the block. I've seen this before.
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Offline larrym

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Wasted main
« Reply #10 on: October 10 2014, 12:23:53 AM »
 I inspected number 3 cap pretty closely it looked ok I did not see any thing that looked chipped cracked or abraded where it fits into register. It was very loose number 2 was tight.
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

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Re: Wasted main
« Reply #11 on: October 10 2014, 12:52:50 AM »
Larry, I saved the 4 main caps from the block I had to scrap last June due to the cracked cylinder. If we haven't sold them...do you want the two center caps? If they aren't sold...you can have 'em.
Hard work pays off, dreams come true. Bad times don't last, but BAD GUYS do!

RIP Scott Hall AKA Razor Ramon

Offline larrym

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Wasted main
« Reply #12 on: October 10 2014, 01:19:23 AM »
Thanks Brad if the block checks out he will probably go with billet caps either way  he would need to have the cap fitted to the block and a line bore. Should know more by the weekend as to what direction he is going to go.
I just want to figure out what happened the block could be a boat anchor.   
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

Offline Scoobum

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Re: Wasted main
« Reply #13 on: October 10 2014, 08:31:21 AM »
Be sure to inspect the new caps for the chamfer to match the block. Bought an engine from one of the locals a few years back. He kept taking the mains out of it on startup...3 times. He reluctantly sold me the engine. Had a look at it...and the two steel center main caps didn't have the chamfer on 'em. His machinist torqued the caps down each time...and align honed it...degreased it...and handed him the block each time. If his machinist had of loosened the caps and then retorqued them and rechecked...li ke your suppose to after and align hone/bore...he would have noted they were tight/loose all over the place like I did when I checked them. I took the caps/block to a friends machine shop and had the caps machined to fit the block...and had an align hone done. Engine is still in service to this day.
Hard work pays off, dreams come true. Bad times don't last, but BAD GUYS do!

RIP Scott Hall AKA Razor Ramon

Offline larrym

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Re: Wasted main
« Reply #14 on: October 10 2014, 04:29:24 PM »
So would a couple backfires from a bad coil pack be enough to bend a crank?
He is going to check the crank tonight, if it was bent that would explain the hammered cap pulling the edges out of the register or would the heat be enough to distort the cap, its not blued.
86 white T type with t tops and blackout trim. 60lb injectors Gen 2 with Extender Chip TR6 ignition 212/206 roller cam Turbonetics BB CPT 61 CAS V4 Intercooler Cobbled together Alky Injection 4 inch MAF pipe with integral sensor
2800 stall lots of fun with a little 6 banger!
Best ET 11.36

 

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