This TR has other issues and I had the owner send Eric the PL file to get his opinion as well...the file's a mess. I'm not sure how the head gaskets are still in it. Anyway, leaving the line the boost is 4 psi...and 7 seconds later down the track it makes its way up to 20 psi...and takes another 3 seconds to move up to 23 psi...and then moves around from 24 to 25.9 psi to the 1/4 mark. The convertor is spec'd for the turbo...so he's removing the external gate and handing it to someone I trust for inspection. With the boost fluttering in high gear...and the KR I'm seeing from start to finish, I suspect the head gaskets are starting to leak. First things first. What's your thots on the boost taking forever to rise.